After finding nothing dramatic wrong other than expected wear and tear, a second opinion review of the parts from an engineer mate, I've got some fresh (hepolite rings, had the bores honed and as there was some oil seep from the pushrod area on the head gasket, skimmed the barrel. Will also reassemble head and bang it back together. Have just bought a small ultrasonic cleaner as looking to try some concentrics, have a matched set of 30mm or a pair of LH 32's (might be hard to adjust) and probably run this season on avgas.
Would have liked some 3 piece oil rings but the hepolites were readily available and it will get a hard run in .
Fairings also get some further repair and will cut it down a bit.
I think the next time this motor comes down it'll be due for new rods etc, but its done very well for a road based designed motor not usually considered to be that robust. It's taken a lot of stick and outperformed my expectation.
I'm thinking that its next incarnation might be with an alloy barrel and nikasil bores for close clearances, perhaps a65 cams and followers
, scheming is underway. But thats next year if I'm lucky.
Have also entered the NZCMRR pukekohe classic Festival early Feb