Hello Muskrat, here in Cranbourne, 35km southeast of Melbourne. Previous owner rebuilt the engine from the crank up. Sent the crank away to get the required end float exact, SRM 8.5:1 pistons (clearance unknown), new valve guides & valves (told me the guides are a tight fit to Ensure no blow by, as engine used to be a smoker) & geared it up one tooth on the front as it pulled so well after the overhaul. Dynamo rewound, 12 volt system, thorspark ignition etc etc etc. After the 2nd seize, I cleaned out the fuel tank (some small flakes of debris inside), replaced a clogged inline fuel filter, which I suspected was causing it to lean out & ping plus found the needle jet loose in the carby. All fixed & back together but seized again yesterday Disappointing.